Right I've just spent 4 hours faffing
I've just lagged the charge cooler
Now we undone most of the bolts on the down pipe and used a screw driver as a lever on the down pipe.
No noise was evident of the waste gate snapping shut.
I could not see the waste gate so have no idea if it was open.
what I did find was a pipe from the actuator that has been capped off. The plastic cap had been badly heat damaged and was crumbling away in my hand.
I didn't have anything to had so had to Bodge it for now with RTV sealant.
Now generally I can hit 8 psi really easy. However when I last drove the car it was really hard to get boost. I virtually had to redline the car.
Ill be taking the car out later to see what happens then.